Hi, I’m having a serious problem with my VESC build and wonder if someone has made the same experiences/knows a solution to it:
I run a single mounted 270KV motor with an 8S LiPo (2x4S in series), and I use VESC in BLDC mode. I used the BLDC tool to set all up. I skated with it about a 100 km without any problems. However, from one moment to the other while cruising, the break kicked in and threw me off my board (no injuries) - very scary! I first though I unintentionally hit the break. However, after running smooth for some time after it happened again and I’m sure VESC is hitting the break without me actively breaking. Does anyone have made the same experiance? Is it possible that motor parameters change over time due to wearing and rerunning a detection can solve this? It’s quite scary since there is no good testing methods that guarantees that the problem is resolved.
- Remote: http://alienpowersystem.com/shop/radio-transmitters/alien-power-system-2-4ghz-electric-skateboard-remote-control/
- VESC: version 4.12; firmware version 2.18