I have a FOCBOX Unity with dual Torque Boards 6355’s and I’m running BLDC. I just finished my build with the Unity and I’m having some issues. When I’m at a stand still I have this problem where my motors will shake and then slowly start running backwards at a set speed regardless of throttle. If I let off and push off it will go forward alright. I know shaking is normal if you don’t push off with BLDC but yeah this seems not normal. I had two TB VESC’s before this and they needed slightly less of a push off and didn’t do this weird reverse thing. Any help would be great!
I included a YouTube link, please let me know what you think.
I haven’t used the app yet, but I feel like the desktop is easier no matter what, the app is probably better in the end for quick adjustments rather than first time setup.
You can view all of your settings in the desktop app, as long as you remember to click the read settings from VESC button
Hey so the desktop app is the same as the android app. At this point I set it up correctly with one of the Enertion staff and it still does it. I think the only thing to do at this point is to get sensor wires so I can run sensored FOC I think that’d fix it.